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Capacitor Discharging with CMOS Gate

D

D from BC

Is this safe to do?

4093 Cmos Schmitt NAND
_
-------| \ <<<discharging
| |0--|<--+
-------|_/ |
--- Initially at 14V
--- 10uF tantalum
|
com

Repetition rate: 6Hz

On the datasheet
http://www.onsemi.com/pub/Collateral/MC14093B-D.PDF
The max output current spec is 10mA.

But I think that spec is continuous current.
Impulse current and internal impulse power is another thing.
Could a die wire pop?
Could the drive mosfet fry?

I'm trying to dodge including a current limiting resistor.
Extra part, extra pcb space, extra drafting...that sort of thing.


D from BC
British Columbia
Canada.
 
J

John Larkin

Is this safe to do?

4093 Cmos Schmitt NAND
_
-------| \ <<<discharging
| |0--|<--+
-------|_/ |
--- Initially at 14V
--- 10uF tantalum
|
com

Repetition rate: 6Hz

On the datasheet
http://www.onsemi.com/pub/Collateral/MC14093B-D.PDF
The max output current spec is 10mA.

But I think that spec is continuous current.
Impulse current and internal impulse power is another thing.
Could a die wire pop?
Could the drive mosfet fry?

I'm trying to dodge including a current limiting resistor.
Extra part, extra pcb space, extra drafting...that sort of thing.


D from BC
British Columbia
Canada.

No problem.

John
 
D

D from BC

No problem.

John

Cool thanks..
Wonderful...That's one less part for my life support system circuit..
:p
(Just kidding..)


D from BC
British Columbia
Canada.
 
J

JosephKK

D said:
Cool thanks..
Wonderful...That's one less part for my life support system circuit..
:p
(Just kidding..)


D from BC
British Columbia
Canada.

I am not so cheerful about it. It looks to me that there can be a
localized heating reliability problem with the CMOS gate output pin.
 
W

Winfield

JosephKK said:
I am not so cheerful about it. It looks to me that there can be a
localized heating reliability problem with the CMOS gate output pin.

During the 10uF capacitor's discharge from 14V
the 4093 gate's n-channel output mosfet has to
dissipate 1mJ of energy in 5ms (assuming a 25mA
discharge current). Doing this six times a
second means the gate's die will dissipate 6mW,
which is certainly not a problem, but this fails
to fully settle the question of whether a 350mW
peak power level will be damaging.

D can try an acid test, by continuously running
the output at full current and supply voltage,
and testing for any reduction in the IC's life.

4093 CMOS Schmitt NAND - acid test,
_
+14 --+--| \
| | |0--- +14V
'--|_/

We assume the 4093 is powered from the +14V.

The IC's datasheet says the Absolute Maximum
package power dissipation is 500mW, at room temp,
which implies 350mW will run the die temperature
near the maximum rated value. That's not a very
good idea, but it may be tolerated OK for a few
ms every 167ms.

I'd add the series resistor myself.
 
S

Spehro Pefhany

During the 10uF capacitor's discharge from 14V
the 4093 gate's n-channel output mosfet has to
dissipate 1mJ of energy in 5ms (assuming a 25mA
discharge current). Doing this six times a
second means the gate's die will dissipate 6mW,
which is certainly not a problem, but this fails
to fully settle the question of whether a 350mW
peak power level will be damaging.

D can try an acid test, by continuously running
the output at full current and supply voltage,
and testing for any reduction in the IC's life.

4093 CMOS Schmitt NAND - acid test,
_
+14 --+--| \
| | |0--- +14V
'--|_/

We assume the 4093 is powered from the +14V.

The IC's datasheet says the Absolute Maximum
package power dissipation is 500mW, at room temp,
which implies 350mW will run the die temperature
near the maximum rated value. That's not a very
good idea, but it may be tolerated OK for a few
ms every 167ms.


Metal migration induced failures?

Note: abs. max "Input or Output Current
(DC or *Transient*) per Pin 10mA)

(emphasis added)
I'd add the series resistor myself.

Indeed. Particularly with a 15V supply. Sink current is off the gaph
(> abs max) at less than 2V Vds.
Best regards,
Spehro Pefhany
 
F

Fred Bloggs

Spehro said:
Metal migration induced failures?

Note: abs. max "Input or Output Current
(DC or *Transient*) per Pin 10mA)

(emphasis added)

I don't think that process has the capability to induce metal migration,
too weak...20mA never burned up anything.
Indeed. Particularly with a 15V supply. Sink current is off the gaph
(> abs max) at less than 2V Vds.
Best regards,
Spehro Pefhany

May be off the graph, but you can see the (Vgs-Vth)^2 characteristic
across the Vgs, so that 1.75mA @ 5V => Vth~1.35V and 25mA@Vgs=15V, which
is about in line with the curvatures shown there. This makes for 350mW
peak and 6msec discharge time for 4% duty. It shouldn't be a problem. He
gets about the same discharge time with a series 330R, current peak will
be about the same, but peak power reduces to <150mW.
 
D

D from BC

During the 10uF capacitor's discharge from 14V
the 4093 gate's n-channel output mosfet has to
dissipate 1mJ of energy in 5ms (assuming a 25mA
discharge current). Doing this six times a
second means the gate's die will dissipate 6mW,
which is certainly not a problem, but this fails
to fully settle the question of whether a 350mW
peak power level will be damaging.

D can try an acid test, by continuously running
the output at full current and supply voltage,
and testing for any reduction in the IC's life.

4093 CMOS Schmitt NAND - acid test,
_
+14 --+--| \
| | |0--- +14V
'--|_/

We assume the 4093 is powered from the +14V.

The IC's datasheet says the Absolute Maximum
package power dissipation is 500mW, at room temp,
which implies 350mW will run the die temperature
near the maximum rated value. That's not a very
good idea, but it may be tolerated OK for a few
ms every 167ms.

I'd add the series resistor myself.

Yup.. Vdd=14V.

Mmmm.. I might test.. I'm thinking about it..
Testing SOIC chips are a pita without a breakout board..

I think this is one of those problems where the datasheet can't
provide every detail, the testing is a pita and putting in a current
limiting resistor is the easy way out.

I'm still learning that sometimes it's just not worth the time to
dodge only one resistor in a circuit and accept more risk.
On the other side, it's artsy to dodge a 'be kind to mosfets'
resistor. :)

So yeah say use the resistor ... :)


D from BC
British Columbia
Canada.
 
D

D from BC

Metal migration induced failures?

Note: abs. max "Input or Output Current
(DC or *Transient*) per Pin 10mA)

(emphasis added)


Indeed. Particularly with a 15V supply. Sink current is off the gaph
(> abs max) at less than 2V Vds.
Best regards,
Spehro Pefhany


I think the absolute max 'transient' note is conservative when it
equals the DC absolute max current.
However I'm thinking it's not worth the risk to find out.


D from BC
British Columbia
Canada.
 
J

JosephKK

Fred said:
I don't think that process has the capability to induce metal migration,
too weak...20mA never burned up anything.

Actually, even uA currents induce metal migration. Some 30 years ago
there was a recognized IC failure mode called Kirkendall voiding.
Please Google before calling me a fool.
May be off the graph, but you can see the (Vgs-Vth)^2 characteristic
across the Vgs, so that 1.75mA @ 5V => Vth~1.35V and 25mA@Vgs=15V, which
is about in line with the curvatures shown there. This makes for 350mW
peak and 6msec discharge time for 4% duty. It shouldn't be a problem. He
gets about the same discharge time with a series 330R, current peak will
be about the same, but peak power reduces to <150mW.

This is getting interesting enough that i must ask someone who has
access to decent test equipment to make some measurements. After 13
years in test labs and 15 years in a job where test instruments are
irrelevant i am down to a DMM. Se le guerre.
 
F

Fred Bloggs

JosephKK said:
Actually, even uA currents induce metal migration. Some 30 years ago
there was a recognized IC failure mode called Kirkendall voiding. Please
Google before calling me a fool.

Metal migration has to do with extraordinarily large current densities
and not power dissipation. Those weak little CMOSFETs in the 14000
process can't do it, even the AC family can't do it.
 
J

Joerg

John said:
No problem.

If VCC briefly dips for some reason and the cap had enough charge the
whole thing might go into latch-up. That would not be cool.
 
J

Jim Thompson

On Thu, 21 Feb 2008 20:14:43 GMT, Joerg

[snip]
If VCC briefly dips for some reason and the cap had enough charge the
whole thing might go into latch-up. That would not be cool.

Actually that WOULD be cool ;-)

...Jim Thompson
 
J

Jim Thompson

On Thu, 21 Feb 2008 20:14:43 GMT, Joerg

[snip]
If VCC briefly dips for some reason and the cap had enough charge the
whole thing might go into latch-up. That would not be cool.

Actually that WOULD be cool ;-)

...Jim Thompson

An open-drain-output would most likely be safe, since their ESD is
usually only an N-channel device, thus not path to VDD.

...Jim Thompson
 
D

D from BC

On Thu, 21 Feb 2008 20:14:43 GMT, Joerg

[snip]
If VCC briefly dips for some reason and the cap had enough charge the
whole thing might go into latch-up. That would not be cool.

Actually that WOULD be cool ;-)

...Jim Thompson

Huh? Latch up?
The gate is shunting the charged cap to ground.
(Charging circuit not shown for clarity)
Ideally, I think this shouldn't have an effect on the rails.
Non-ideally..
What's it called...ground bounce??
The cap dumps through the gate and blips the Vss rail.


D from BC
British Columbia
Canada.
 
D

Dave Platt

Huh? Latch up?
The gate is shunting the charged cap to ground.
(Charging circuit not shown for clarity)
Ideally, I think this shouldn't have an effect on the rails.
Non-ideally..
What's it called...ground bounce??
The cap dumps through the gate and blips the Vss rail.

Driving the output of a logic gate too far outside the rail voltage
can trigger a latchup. This can happen with as little as one
diode-drop of excessive voltage. The overvoltage/spike has the effect
of activating a "parasitic" structure on the die (a set of P/N
junctions not normally part of the circuit, but created in part as a
side effect of the way the die is fabricated). If you're unlucky, the
parasitic junctions form a PNPN structure, a.k.a. a thyristor or SCR.
The spike "turns on" this thyristor, and it begins acting as a short
circuit which often can't be reset by any means less drastic than
turning off the power entirely.

If the source of the overvoltage has enough charge it and a low enough
impedance, the resulting current flow through the parasitic can
destroy the chip.

I heard a tale some years ago about an incident involving a new,
prototype RISC CPU. The first silicon had just come back from the
fab, in one of the special ceramic packages with a quartz lid (to
allow for inspection of the chip). Chip was carefully powered up, and
lo and behold it worked! One of the developers was so proud that he
whipped out a camera and took a photo of the chip in the development
board.

Bad move. The camera's flash fired. The flash emitted enough UV
(which went through the flash's lens, and through the clear quartz lid
of the chip) to cause photoelectric-effect activation of a bunch of
the exposed gates on the surface of the chip - a bunch of electrons
got knocked loose by the bright light. A whole bunch of parasitic
thyristor structures turned on, and (in effect) short-circuited the
power supply to ground on multiple places on the chip.

The camera's flash was followed, with no perceptible delay, by a
bright flash _inside_ the chip's lid. Boom. Completely dead chip.
Do not pass Go, do not collect $200, no saving throw possible.
 
J

Joerg

D said:
On Thu, 21 Feb 2008 20:14:43 GMT, Joerg

[snip]
If VCC briefly dips for some reason and the cap had enough charge the
whole thing might go into latch-up. That would not be cool.
Actually that WOULD be cool ;-)

...Jim Thompson

Huh? Latch up?
The gate is shunting the charged cap to ground.
(Charging circuit not shown for clarity)
Ideally, I think this shouldn't have an effect on the rails.
Non-ideally..
What's it called...ground bounce??
The cap dumps through the gate and blips the Vss rail.

Depends on what else is hooked up to that rail. Assume the cap is full.
Now some big fat load dips that rail a little. Phssst ... POOF.
 
J

Joerg

Dave said:
Driving the output of a logic gate too far outside the rail voltage
can trigger a latchup. This can happen with as little as one
diode-drop of excessive voltage. The overvoltage/spike has the effect
of activating a "parasitic" structure on the die (a set of P/N
junctions not normally part of the circuit, but created in part as a
side effect of the way the die is fabricated). If you're unlucky, the
parasitic junctions form a PNPN structure, a.k.a. a thyristor or SCR.


On CD4000 logic that is usually the case.

The spike "turns on" this thyristor, and it begins acting as a short
circuit which often can't be reset by any means less drastic than
turning off the power entirely.

If the source of the overvoltage has enough charge it and a low enough
impedance, the resulting current flow through the parasitic can
destroy the chip.

Once the parasitic SCR has been triggered the impedance of the source
doesn't matter anymore. You could completely remove it and the chip
would remain in meltdown mode anyhow if the supply rail has enough
juice. A loud bang, a stench, smoke alarms wailing, and so on.

I heard a tale some years ago about an incident involving a new,
prototype RISC CPU. The first silicon had just come back from the
fab, in one of the special ceramic packages with a quartz lid (to
allow for inspection of the chip). Chip was carefully powered up, and
lo and behold it worked! One of the developers was so proud that he
whipped out a camera and took a photo of the chip in the development
board.

Bad move. The camera's flash fired. The flash emitted enough UV
(which went through the flash's lens, and through the clear quartz lid
of the chip) to cause photoelectric-effect activation of a bunch of
the exposed gates on the surface of the chip - a bunch of electrons
got knocked loose by the bright light. A whole bunch of parasitic
thyristor structures turned on, and (in effect) short-circuited the
power supply to ground on multiple places on the chip.

The camera's flash was followed, with no perceptible delay, by a
bright flash _inside_ the chip's lid. Boom. Completely dead chip.
Do not pass Go, do not collect $200, no saving throw possible.

What did they do with the guy?
 
D

D from BC

Driving the output of a logic gate too far outside the rail voltage
can trigger a latchup. This can happen with as little as one
diode-drop of excessive voltage. The overvoltage/spike has the effect
of activating a "parasitic" structure on the die (a set of P/N
junctions not normally part of the circuit, but created in part as a
side effect of the way the die is fabricated). If you're unlucky, the
parasitic junctions form a PNPN structure, a.k.a. a thyristor or SCR.
The spike "turns on" this thyristor, and it begins acting as a short
circuit which often can't be reset by any means less drastic than
turning off the power entirely.

If the source of the overvoltage has enough charge it and a low enough
impedance, the resulting current flow through the parasitic can
destroy the chip.

I heard a tale some years ago about an incident involving a new,
prototype RISC CPU. The first silicon had just come back from the
fab, in one of the special ceramic packages with a quartz lid (to
allow for inspection of the chip). Chip was carefully powered up, and
lo and behold it worked! One of the developers was so proud that he
whipped out a camera and took a photo of the chip in the development
board.

Bad move. The camera's flash fired. The flash emitted enough UV
(which went through the flash's lens, and through the clear quartz lid
of the chip) to cause photoelectric-effect activation of a bunch of
the exposed gates on the surface of the chip - a bunch of electrons
got knocked loose by the bright light. A whole bunch of parasitic
thyristor structures turned on, and (in effect) short-circuited the
power supply to ground on multiple places on the chip.

The camera's flash was followed, with no perceptible delay, by a
bright flash _inside_ the chip's lid. Boom. Completely dead chip.
Do not pass Go, do not collect $200, no saving throw possible.

Afterward, did that developer go to the bar and got drunk?
"ssshhhupid flashh... Friffffn flashh... Yah know..I...I ...I... never
takn anoother picture in my liffee" :p


D from BC
British Columbia
Canada.
 
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